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AD 76-11-06 ACTIVE

Switch Bus Bar Link
Key Information
AD Number 76-11-06 Status Active
Effective Date June 04, 1976 Issue Date May 21, 1976
Docket Number Unknown Amendment 39-2629
Product Type ["Aircraft"] Product Subtype ["Small Airplane"]
CFR Part --- - Part 39 CFR Section --- - _EMPTY_
Citation This information is not available.
Applicability
Manufacturer(s) Piper Aircraft Inc.
Model(s) PA-31P
Regulatory Text

76-11-06 PIPER: Amendment 39-2629. Applies to Model PA-31P, S/Ns 31P-1 to 31P-7630001 inclusive, and 31P-7630003.

Compliance required within the next 100 hours in service after the effective date of this AD unless already accomplished.

To prevent the hazards associated with the possibility of the alternator switch bus bar link shorting to the adjacent fuselage bulkhead, accomplish the following:

(a) Alter the existing switch bus bar link insulation in accordance with the "Instructions" paragraph in Service Bulletin No. 473, dated March 24, 1976, or with an approved alternate method.

(b) Upon request with substantiating data submitted through an FAA Maintenance Inspector, the compliance time specified in this AD may be increased by the Chief, Engineering and Manufacturing Branch, FAA Eastern Region who must also approve any alternate alteration.

This amendment is effective June 4, 1976.

Office of Primary Responsibility
["AIR-720: Operational Safety Branch"]