| AD Number | 61-21-05 | Status | Active |
| Effective Date | November 02, 1961 | Issue Date | Not specified |
| Docket Number | Unknown | Amendment | N/A |
| Product Type | ["Aircraft"] | Product Subtype | ["Large Airplane"] |
| CFR Part | --- - Part 39 | CFR Section | N/A |
| Citation | This information is not available. | ||
| Manufacturer(s) | Lockheed Martin Corporation |
| Model(s) | 188A 188C |
61-21-05 LOCKHEED: Amdt. 342 Part 507 Federal Register October 3, 1961. Applies to All Model 188 Aircraft.
Compliance required as indicated.
Several instances of inadvertent tripping of compass circuit breakers have occurred due to bumping the ganging bar by the occupant of the observers seat. Due to the effect of the loss of heading information upon operational safety, accomplishment of the following is required:
Within the next 100 hours' time in service after the effective date of this AD, inspect the pilot's and copilot's compass circuit breakers, and if the circuit breakers are ganged together, either remove the ganging bars, or install a protective guard which precludes inadvertent operation of the ganging bar. (These circuit breakers are located in the lowest circuit breaker panel beside the observers seat on the left side of the flight deck.)
This directive effective November 2, 1961.