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AD 77-02-07 ACTIVE

Propeller Feathering
Key Information
AD Number 77-02-07 Status Active
Effective Date March 01, 1977 Issue Date Not specified
Docket Number Unknown Amendment 39-2817
Product Type ["Aircraft"] Product Subtype ["Small/Large Airplane"]
CFR Part --- - Part 39 CFR Section N/A
Citation This information is not available.
Applicability
Manufacturer(s) Textron Aviation Inc.
Model(s) 200
Regulatory Text

77-02-07 BEECH: Amendment 39-2817. Applies to Model 200 (Serial Numbers BB-2, BB-6 thru BB-18 and BB-20 thru BB-50) airplanes.

Compliance: Required within 100 hours' time in service after the effective date of this AD, unless already accomplished.

To prevent unintentional feathering of a propeller due to failure of the secondary low pitch stop amplifier, accomplish either Paragraph A or B:

A) Replace both P/N 101-364171-1 and P/N 101-364171-9 printed circuit board assemblies with P/N 101-364170-15 printed circuit board assemblies in accordance with Beechcraft Service Instruction No. 0745-354, notwithstanding its supersedence by Beechcraft Service Instruction No. 0808-247.

B) Remove secondary low pitch stop system in accordance with Beechcraft Service Instruction No. 0808-247, or later approved revisions.

C) Airplanes which have accumulated 100 hours' time in service after the effective date of this AD may be flown in accordance with FAR 21.197 to a place where a replacement or removal can be performed, providing the existing amplifiers have not malfunctioned.

D) Any equivalent method of compliance with this AD, must be approved by the Chief, Engineering and Manufacturing Branch, FAA Central Region.

NOTE: The manufacturer has advised the FAA that sufficient replacement parts are available to accomplish Paragraph A of this AD.

This amendment becomes effective March 1, 1977.