| AD Number | 80-20-06 | Status | Active |
| Effective Date | October 14, 1980 | Issue Date | Not specified |
| Docket Number | Unknown | Amendment | 39-3937 |
| Product Type | ["Aircraft"] | Product Subtype | ["Small Airplane"] |
| CFR Part | --- - Part 39 | CFR Section | N/A |
| Citation | This information is not available. | ||
| Manufacturer(s) | Cessna Aircraft Company |
| Model(s) | 421C |
80-20-06 CESSNA: Amendment 39-3937. Applies to Model 421C airplanes (Serial Number 421C0401 and on) having King KFC-200 Flight Control System installed under Supplemental Type Certificate SA1246CE.
COMPLIANCE: Required as indicated unless already accomplished.
To prevent the airplane from exceeding 60 degrees bank angle in the event of a roll axis hard-over malfunction, accomplish the following:
A) Within the next 25 hours time-in-service after the effective date of this AD, reset the KFC-200 roll axis slip clutch from 60 plus or minus 6 inch-pounds to 38 plus or minus 4 inch-pounds in accordance with the instructions contained in King Radio Service Sales Installation Bulletin No. 167 dated August 4, 1980.
B) Airplanes may be flown in accordance with FAR 21.197 to a location where the maintenance required by this AD may be performed provided the autopilot is inoperative.
C) Any equivalent method of compliance must be approved by the Chief, Aircraft Certification Program, Federal Aviation Administration, Room 238, Terminal Building No. 2299, Mid-Continent Airport, Wichita, Kansas 67209.
This amendment becomes effective October 14, 1980.