AD 90-24-04

Active

Outboard Flap Inspection

Key Information
90-24-04
Active
December 24, 1990
Not specified
90-NM-95-AD
39-6809
Applicability
["Aircraft"]
["Large Airplane"]
The Boeing Company
737-200 Series 737-300 Series 737-400 Series
Regulatory Text

90-24-04 BOEING: Amendment 39-6809. Docket No. 90-NM-95-AD. \n\n\tApplicability: Model 737-200 series airplanes, listed in Boeing Alert Service Bulletin 737-57A1206, dated April 12, 1990; and Model 737-300 and 737-400 series airplanes, listed in Boeing Alert Service Bulletin 737-57A1208, dated March 29, 1990; certificated in any category. \n\n\tCompliance: Required as indicated, unless previously accomplished. \n\n\tTo prevent fastener fracture in the fitting attachment which could result in a loss of the outboard flap, accomplish the following: \n\n\tA.\tPrior to the accumulation of 5,000 flight hours or within 12 months after the effective date of this AD, whichever occurs later, perform a visual inspection of the outboard flap support fitting attach bolts in accordance with Boeing Alert Service Bulletin 737-57A1206, dated April 12, 1990, or Boeing Alert Service Bulletin 737-57A1208, dated March 29, 1990, as applicable. \n\n\t\t1.\tIf the bolts are confirmed as BACB30LE6 or BACB30US6,no further action is required at that location. \n\n\tNOTE: A bolt head marking of BACB30LE6, BACB30US6, B30LE6, or B30US6 confirms the correct bolt installation. Oversize bolts BACB30LE7 or BACB30US7 may be installed and are acceptable. \n\n\t\t2.\tIf a bolt BACB30MT is found, prior to further flight, and thereafter at intervals not to exceed 1,000 flight hours, perform torque inspections in accordance with Boeing Alert Service Bulletin 737-57A1208, dated March 29, 1990, or Boeing Alert Service Bulletin 737-57A1206, dated April 12, 1990, as applicable. If the bolt turns at or below the specified torque range, prior to further flight, replace it with BACB30LE or BACB30US in accordance with the previously mentioned service bulletins. Replacement of any bolt with bolt BACB30LE or BACB30US constitutes terminating action for the repetitive torque inspections for that bolt. \n\n\t\t3.\tIf a bolt other than the one listed in paragraph A.1. or A.2. of this AD is found, prior to further flight,replace the bolt with bolt BACB30LE or BAC30US in accordance with Boeing Alert Service Bulletin 737-57A1208, dated March 29, 1990, or Boeing Alert Service Bulletin 737-57A1206, dated April 12, 1990, as applicable. \n\n\tB.\tAn alternate means of compliance or adjustment of the compliance time, which provides an acceptable level of safety, may be used when approved by the Manager, Seattle Aircraft Certification Office, FAA, Transport Airplane Directorate. \n\n\tNOTE: The request should be submitted directly to the Manager, Seattle Aircraft Certification Office (ACO), and a copy sent to the cognizant FAA Principal Inspector (PI). The PI will then forward comments or concurrence to the ACO. \n\n\tC.\tSpecial flight permits may be issued in accordance with FAR 21.197 and 21.199 to operate airplanes to a base in order to comply with the requirements of this AD. \n\n\tAll persons affected by this directive who have not already received the appropriate service documents from the manufacturer mayobtain copies upon request to Boeing Commercial Airplane Group, P.O. Box 3707, Seattle, Washington 98124. These documents may be examined at the FAA, Northwest Mountain Region, Transport Airplane Directorate, 1601 Lind Avenue S.W., Renton, Washington. \n\n\tThis amendment (39-6809, AD 90-24-04) becomes effective on December 24, 1990.

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References
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FAA Documents